Below is the Event Report from the NRC website.
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Facility: ARKANSAS NUCLEAR
Region: 4 State: AR
Unit: [1] [2] [ ]
RX
Type: [1] B&W-L-LP,[2] CE
NRC Notified By: PHILLIP FORE
HQ OPS
Officer: HOWIE CROUCH
Notification Date: 03/31/2013
Notification Time: 11:57 [ET]
Event Date:
03/31/2013
Event Time: 10:33 [CDT]
Last Update Date: 03/31/2013
Emergency Class: UNUSUAL EVENT
10 CFR Section:
50.72(a) (1) (i) -
EMERGENCY DECLARED
50.72(b)(2)(iv)(B) - RPS ACTUATION -
CRITICAL
50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION
50.72(b)(2)(xi) -
OFFSITE NOTIFICATION
NOTIFICATION OF UNUSUAL EVENT DECLARED DUE TO A BREAKER EXPLOSION IN THE
PROTECTED AREA
"At 0750 [CDT] on 3/31/2013, during movement of the Unit
1 Main Turbine Generator Stator (~500 tons), the Unit 1 turbine temporary lift
device failed. This caused a loss of all off site power on Unit 1. The ANO Unit
1 #1 and #2 EDG [Emergency Diesel Generator] have started and are supplying A-3
4160V switchgear and A-4 4160V switchgear. P-4A Service Water pump and P-4C
Service Water pump has been verified running. Unit 1 has entered [procedures]
1202.007 - Degraded Power, 1203.028 - Loss of Decay Heat, and 1203.050 - Spent
Fuel Emergencies. Unit 1 is in MODE 6.
"ANO-1 entered TS 3.8.2 A, 'One
Required Offsite Circuit Inoperable'. All required actions are complete. The
event caused a loss of decay heat removal on ANO Unit 1 which was restored in 3
minutes and 50 seconds.
"Unit 2 tripped and is in MODE 3. Emergency Feed
Water was initiated on Unit 2 and Unit 2 was in [Technical Specification] 3.0.3
from 0817 [CDT] to 0848 [CDT] due to Emergency Feedwater. Unit 2 is being
powered by off-site. Unit 2 Startup 3 [transformer] lock out at 0921 [CDT].
[Bus] 2A1 is on Start up 2 [transformer] and [bus] 2A3 is on #2 EDG.
"10CFR50.72 (b)(3)(iv)(A) - 4-hr. notification due to the ES [Engineered
Safeguard Feature] actuation on both Unit 1 and Unit 2.
10CFR50 72
(b)(2)(iv)(B) - 4-hr. notification due to RPS [Reactor Protection System]
actuation on Unit 2.
10CFR50.72 (b)(2)(xi) - 4-hr. notification due to
Government Notification.
29CFR1904.39a - [OSHA] 8-hr. notification due to
death on site.
"At 1033 [CDT] on 3/31/2013, Unit 2 entered a
Notification of Unusual Event based on EAL HU4 due to damage in 2A1 switchgear.
Notification of the NUE will be made lAW Emergency Plan requirements. Follow-up
notifications will be made as appropriate."
At this time, the full
extent of structural damage on Unit 1 is not known. There was one known fatality
and 4 known serious injuries to workers. The local coroner is on site for the
fatality and the injured personnel have been transported offsite to local
hospitals. Investigation into the cause of the failure and extent of damage is
ongoing.
On Unit 2, all rods inserted during the trip. The core is being
cooled via natural circulation. Decay heat is being removed via steam dumps to
atmosphere. There is no known primary to secondary leakage.
The licensee
has notified the State of Arkansas, local authorities, OSHA and the NRC Resident
Inspector.
Notified DHS SWO, DHS NICC, FEMA and Nuclear NSSA (via
email).
* * * UPDATE FROM DAVID THOMPSON TO HOWIE CROUCH AT 1934 EDT ON
3/31/13 * * *
The licensee terminated the NOUE at 1821 CDT. The basis
for termination was that the affected bus (2A2) is de-energized and no other
equipment on Unit 2 was damaged.
The licensee has notified the state and
local authorities and will be notifying the NRC Resident Inspector.
Notified R4DO (Pick), NRR EO (Howe), IRD (Gott), DHS SWO, DHS NICC, FEMA
and Nuclear SSA (via email).
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